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NickySB

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Posts posted by NickySB

  1. a little update - the garage maintained they couldn’t possibly be to blame, however when I asked them to clarify why they felt the issues and the repairs weren’t linked they couldn’t.  After an extra week they finally returned the car. I’ve agreed an independent specialist will investigate the issues and report on them accordingly, and if a link is confirmed I expect them to pay for the repair.  Specialist has some holiday booked so will have to wait at least another week or so but the car has been taken to them via a transporter.

  2. 34 minutes ago, steve2006 said:

    I don’t see how they can deny responsibility for the battery damage when it was driven to them and needed to be driven inside for the MOT.

    It got to be top of the list when welding a vehicle.....always disconnect the battery which I would assume includes the hybrid pack.

    Yes agreed completely - just waiting to hear what their plan is and when it’s coming back to me but after it being off the road for a year I’m so upset I can’t finally drive it 😭

  3. Well this really is the gift that keeps on giving! After doing the other work the car was ready for a MOT but needed a bit of welding on the rear sills. Sent it to a local garage as my welder is in storage at the moment and that has turned out to be a bad decision. Whilst they’ve done the welding and the MOT, I believe they’ve also fried the hybrid Battery so now it won’t start ( the usual check hybrid system, check ECB and no ‘ready’).  It drove down there no problem at all. 
    I’m waiting for them to deliver the car back to me whilst we have some strong discussions in the background. They are declining it was their doing, but the fact remains it went in find with no issues or codes and has come out very broken. 

     

    • Sad 1
  4. Another update - cells all balanced - checked the discharge on them and 3 cells identified as discharging too quickly so changed those too. Hybrid Battery back in. Car runs well without any warnings or codes. I’m a little concerned by the lack of electricity flow on the central screen however I’m out of MOT so can’t go for a drive yet. Got a couple of unrelated things to resolve before it goes for a test, will be able to determine once it’s passed whether it then recharges properly. 

    • Like 1
  5. Still have hybrid issues - took the Battery apart ( this is the 3rd time ) - found the corrosion again on the washers. Cleaned them all up- all cells checked out but they’re all ready unusually high- 8.12-8.16v.

    I’ve not seen the hybrid cells that high before- it’s normally 7.7 ish. After reinstalling still got the EML, warning trainable, check hybrid system, EBC & VSC. In my prior experience these normally indicate the hybrid Battery has at least one duff cell or corrosion- but having covered that off I am a little concerned by the higher voltage- investigation continues….don’t have a TechStream sadly

  6. Hi - I think it the timing jumped - exact cause unknown- maybe the chain stretching or maybe related to the issues we experienced with the water pump- and I never found the piston/conrod damage on the first rebuild as I never looked that deep- isn’t hindsight wonderful 😂 I also think that has already happened before the rebuild as it didn’t run long enough or well enough to do that damage afterwards. We’re just at the point of doing coolant/oil refills then we will see what she does - keep everything crossed for me pls ☺️🤞🏻

    • Like 2
  7. Reconnecting the transmission to the replacement engine took at little while due to having limited facilities to get both units at the exact same height- another afternoons work. Spent another 3-4 hrs prepping the replacement engine - changing any broken cables or damaged parts and changing some consumables. 
    Took about another 6 hrs to get the engine and transmission back in together. There’s a lot of fettling as it is a tight space. We came in from the top, and did have to drop the steering rack and subframe a bit ( not remove completely ) and eventually it all slotted into place. Gearbox mount, subframe and steering rack all back on- now to reconnect and rebuild the front end.

     

  8. project engine change is well under way. We decided will will remove/replace via the front end. It took around 3 hrs to get the front end apart with a few tricky rusted bolts but having clear access is much easier. After stripping off the heads it took about another 4 hrs to finish that and get the block separated from the transmission. Transmission out next ( they’ll go back in together ) EDBB44CE-8B72-4E62-9BD3-95388DD69ACF.thumb.jpeg.49dded999785c0d009d1a8a36a01e8f0.jpeg

    • Like 1
  9. I don’t like threads being left unanswered so thought I would update again. Took the rocker covers off again to find the timing had moved. This was odd as we checked the timing 3 times after replacement and rotated the engine by hand with no issues.

    when rotating the engine by hand there was a strange noise that would occur every resolution at a certain point- I can only

    describe it as a high pitch squeal. I then decided to get the crank shield off in the sump and take a look from below. It became clear that during rotation cylinder 4    was generating the noise. On closer inspection it appears to have bent a Conrod- so at least I have a better picture of what’s going on. I’ve decided not to rebuild the existing lump for fear of what other damage may have been caused, so a replacement engine is on standby and I’ll inspect the failure etc in more detail after. If anyone has done a transplant on a 450h and has any tips on the best method of approach please share ☺️

    • Like 2
  10. There was a visible path of oil through the HG , pistons & bores looked ok, but didn’t completely dismantle the engine. I’ve no reason to suspect the little or big ends as the rattle is definitely top end, plus no metal in the oil. When turning the engine over by hand, prior to removing the heads, the valves seemed to operate without issue and they had the TB Mod about 10 yrs ago.

    the timing chain looked to have jumped on removal so I suspected it has just stretched but must be something else going on, and perhaps the clatter that started just before we took it apart was related to the oil issue so just have a more serious oil discrimination issue buried in there somewhere 

  11. Thanks for your input guys, a few good points to think about there - I’ve not got back into it yet due to moving house from one end of the country to the other. I am concerned that the preferred oil (5w30) might be too thin. I had read on the forum before the engine gave me issues that 0w20 was better for these, so I switched to that , and then shortly after started to experience the issues both with coolant and knocking, now it could be completely unrelated , but the fact it’s knocking again after rebuild has me wondering if there is an oil pick up issue somewhere else that I’m missing. I don’t remember any signs of blockage in the pick up tube, the banjo filters are new both sides, and pretty much everything else has been apart. We fitted a new pump at the time of rebuild so shouldn’t be that. I aim to get onto Lexus Tech today and do more research to try and understand the oil system better in its entirety. 

  12. Well the car starts and runs but it’s knocking like a b@stard - valves all looked good on inspection, new chains timing was checked, double checked and treble checked. Installed new oil pump amongst many other new parts. The car is complaining of low oil pressure and other issues but not checked the codes yet.  Suspect the oil Isn’t getting round - it’s got adequate new oil (5w30 as per manual) - anyone got any suggestions on areas of concern pls ? Thanks 

  13. Another mini update- when we got over to the drivers side it had oil in the cylinders so clearly both HGs had failed. I suppose could possibly have been caused by the coolant issues experienced earlier but not definite. Timing chain was also coming out of line so I suspect it had jumped a tooth or two. None of them seemed to be notably different in length when compared to the new ones but they’ve all been replaced for good measure.
    Thankfully no valve damage or head warpage.

    Just completing putting it all back together and replacing the radiator so hopefully it will be running again soon. No doubt the job would have been much easier with the lump out but that sadly wasn’t an option this time. The online manuals have been a god sent ! 

    2FD10759-C4CA-430D-BBB6-3A85F75D2892.jpeg

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