Do Not Sell My Personal Information Jump to content


DanMystro

Members
  • Posts

    35
  • Joined

  • Last visited

Profile Information

  • First Name
    Dan
  • Lexus Model
    LS400
  • Year of Lexus
    2000
  • UK/Ireland Location
    Sussex

Recent Profile Visitors

The recent visitors block is disabled and is not being shown to other users.

DanMystro's Achievements

Explorer

Explorer (4/14)

  • Dedicated Rare
  • One Year In
  • Collaborator
  • Reacting Well Rare
  • First Post

Recent Badges

17

Reputation

  1. Thanks for that info. Yeah in total it was just shy of £800, but I guess cost is subjective.
  2. Awesome stuff to hear! Know if ignition timing gets tampered with?
  3. I know right haha, the centre bit is metal as well.
  4. One other option to control fuelling is to install a wideband to check AFRs and an Apexi Neo SAFC which intercepts the MAF signal and alters it allowing you to adjust the AFR, I've done with my car and it works great, with timing I have not seen any way to do that apart from a standalone ECU.
  5. I use 'buyee', essentially a middle man that let's you browse various Japanese auction sites and shops, once you buy an item it gets shipped to their warehouse where you pay P&P to get it back here. Yes it was Yahoo auction. Cost a lot though 😬
  6. Managed to pick up this TOMs ECU for our facelift LS400s, also came with this sweet Celsior 10th anniversary edition key. Plugged it in and switched key immobiliser chips and starts fine. Just been out for a test drive. It's a lot more responsive now, awesome stuff, I think the fuel map has been changed as well as my wideband is showing slightly richer than before. The rev limit is now 7000 which is awesome! 😃. I read somewhere that on other Toms ECUs for other cars the ignition timing is advanced but I don't know if it's the case on this one, all-in-all great stuff!
  7. Update: Everything back together. Works a dream, even a little better than before! Had a small lumpiness at idle with tiny backfire pre-problem which has now gone away and is smooth as can be, fantastic. When I first started it up after repairs it was smoking quite a bit but I guess that was just condensation buildup and what not from sitting for weeks at an angle, coolant was bubbling out the reservoir which scared me as I thought the head gasket had blown but later realised it was just air burping out the system 😂, silly me. No more smoke and no coolant bubbling, awesome. At this point I'm going to call it a successful job, not much to do now apart from driving it and making sure it all runs right, miss driving the ol' boat so will be a joy to get back behind the wheel. Thanks a lot to everyone for their suggestions and comments! It's been a pain and a pleasure.
  8. Update: Installed the new tensioner, the belt now sits in more (not as close to the edge). The car wouldn't stay running on it's own without my help pressing the throttle down and it would fluctuate the revs up & down, BUT after some fiddling around I finally got it to stay running on it's own, I had to adjust the TPS and play with the throttle motor. I do believe my throttle motor/actuator is dying, normally you hear that slight buzz from the motor but it had no noise coming from it with IGN ON, I had to turn the IGN to OFF and ON a few times for it come on. I have an APEXI NEO installed which measures my throttle position among other things and noticed when the pedal was fully depressed the motor had no power and the butterfly valve only opened a tiny bit due to the wire, after I got the throttle motor to finally turn on and I pressed the pedal I noticed the throttle position had full movement, turned on the car and Boom! It's alive! I won't say it's fixed for now until I reassemble everything and do a little more testing but for now it's looking good.
  9. Sorry for the late reply and thank you. I've got a new tensioner but just waiting for a free day to install it (Friday), when I put the old one back in for testing purposes the rod that pushes up against the tensioner pulley didn't even push the pulley up at all as if it lost all strength, once I fit the new one I should be able to see if there's any difference, I did notice the belt was a bit oily as well which is a cause for slip, so will be checking seals and cam cover rubber seals. I will be re-torquing all bolts to spec again. Nothing looks out of alignment that I could noticeably see.
  10. I did notice after re-timing the cambelt then starting the car the cambelt edged forwards a bit, on the right hand cam gear the belt is literally sitting on the edge of the gear, when I fitted it I pushed it back a bit, I also noticed the belt has moved so much it has edged slighlty off the tensioner idler (If that's what you call it? The bit the tensioner pushes up on). I'm guessing the tensioner is on its way out. Would a weak tensioner be a prime suspect? Thanks for the input, any advice appreciated.
  11. Update: Put the old hydro tensioner on for testing purposes after re-timing the belt, car fires right up (Great! We're getting somewhere) but dies after a second or so, there's next to no fuel in the tank due to draining it to replace the fuel filter so will pour some in tomorrow and give it another go. So far so good but not 100% yet.
  12. To be honest it was me 😂. Although I did it two years ago following a guide to the T, pictures and all, no issues for the last two years until recently when I made this post some weeks ago. I didn't install a new hydro tensioner when I did the work so I'm guessing it just got weaker and weaker over those two years causing it to finally jump. Lesson learnt... Almost done with the work but I'm going to buy a new tensioner and resume once that arrives.
  13. Update: Think I might have found the problem to both the no start and whining noise, took off the right hand cam cover only to find the belt was jumped up over the lip, turned the crank pulley over a few times only to find the belt timing mark(s) are out of alignment with the marks on the cam gear by about six teeth, hopes up! Will be stripping down the front of the engine (Uhh 😪) to re-adjust the belt and pray that was it.
  14. Kind of. Think there's a short in the harness somewhere, managed to get spark and fuel but seems to be starved, FP fine (currently bypassing relay to make sure fuel is constant for testing) , crank and cam sensors fine, changing the fuel filter tomorrow but still need to do a pressure test, codes still there even after switching MAF sensor (24 & 31), could be injectors but not entirely sure, still troubleshooting. My guess is the Ecu isn't getting signals from various sensors.
×
×
  • Create New...